Sunday, March 08, 2009

Fixed … maybe!

I left my camera in Pittsfield, so no pics this week, but we've got the motor all back together, got it running and did NOT hear any sign of the knocking noise. It only ran for 15 minutes or so, but it got plenty warm and previously would have been making the noise under those conditions. So things are looking good and I'm a happy man. We'll see if it holds up over time.

As usual, it wasn't a straight line to assembly. We couldn't get the oil pick up tube and splash pan to align properly - apparently it got bent during removal - so I cannabilized the old '39 engine to see if that tube matched. It did and it's now in the car. We also noticed that the oil pans were the same for both years and that the '39 oil pan was in better shape (the old one had the drain plug repaired and it was obvious). Blasted it clean, painted it and now it's on the car.

What was the source of the noise and how did we fix it? We have no idea, but think it could have been either the broken valve spring dampener or a bearing that didn't sit right in connecting rod #4's bore.

Ken will be finishing up some body work / adjustments and I should have the car back by May 1st. Yeah!

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